How to Fix Synchronous Motor Overheating Problems

Overheating treatment of synchronous motors: First check the load to ensure that it does not exceed the rated value (e.g., the load of a 22kW motor is ≤20kW). Clean the cooling air duct and ensure that the air inlet temperature is ≤40°C. Measure the three-phase current, and the imbalance rate should be <5%. Check the bearing lubrication and replace the high-temperature resistant grease every 2000 hours. Use an infrared thermal imager to locate the hot spot. If the winding temperature exceeds 90°C, shut down the machine for inspection.

Heat Sink Cleaning: Underestimated Overheating Killer

At 3am last November, a 35kW permanent magnet synchronous motor at a Ningbo new energy vehicle parts factory suffered bearing overheating failure, causing ¥157k direct loss. According to National Motor Energy Efficiency Testing Center’s 2023 whitepaper DY2023-EM-044, dust-clogged heat sinks cause 41% of motor unplanned downtime, rising to 68% in foundry and molding workshops.

Our comparative test at a Jiangsu solar panel cleaning equipment factory: Group A’s TEFC motors cleaned quarterly with 0.5MPa compressed air vs Group B’s annual cleaning. After 12 months, Group B’s winding temperature averaged 17℃±3℃ higher than Group A, dropping efficiency from IE4 to IE2.

Cleaning MethodCompressed AirBrush CleaningChemical Cleaning
Cleanliness Recovery82%-95%60%-75%>97%
Residual RisksMay blow dust into bearingsMetal brushes may scratch finsRequires cleaner compatibility verification

Critical alert: A German motor (model omitted) with 2.3mm fin spacing suffered 12% fin deformation from conventional wire brushing, reducing airflow by 40%. Correct method: Use 0.3-0.5MPa dry compressed air at 15° angle along fins—like proper pressure washer angle prevents paint damage.

August 2023 toughest case: Shenzhen smartphone glass CNC motor overheating. 28mg/m³ dust concentration (national standard ≤8mg/m³) with cutting fluid sludge completely blocking heat sinks. Final solution:

  • 60℃ heat gun softens sludge (higher temps damage insulation paint)
  • Food-grade propylene glycol solvent decomposes organics
  • Vacuum removes residues

This combo reduced surface temp from 112℃ to 81℃, saving ¥68k vs replacing housing.

Critical environment factor: At >85% humidity, routine cleaning backfires. Moist dust forms conductive layers, reducing winding-ground insulation resistance by 53%. Solution: Preheat motor surface to dew point +5℃ with infrared heaters before dry cleaning.

Industry trend: Self-cleaning coated heat sinks. Japanese brand’s special oil-repellent material sheds 80% dust automatically, but adds ¥0.8/cm² cost. For 20+ hour/day operation, ROI period 11-14 months—better than most equipment depreciation cycles.

Bearing Lubrication Failure

August 2023 Zhejiang molding plant disaster: ¥4.8M German-made synchronous motor seized, bearing raceways ground metal shavings. Direct loss: ¥198k + efficiency fines. Workshop manager pointed at 112℃ thermometer: “This temp could fry eggs! Where’s the grease?”

Per DY2023-EM-044: Every 10℃ temperature excess exponentially accelerates bearing lifespan decline. Worse, oil starvation causes chain reactions—Suzhou auto parts plant’s SKF 6318 bearing failure recently Burnt stator insulation.

ParameterNormal RangeFault Threshold
Bearing Temp65-85℃>95℃ for 30min
Grease Remnant60-70% housing volume<40% requires immediate refill

Three-step troubleshooting for hot bearings:

  • Quickly touch bearing cover with backhand (beware burns) for heat uniformity
  • Stethoscope detects “click-clack” dry friction sounds
  • Check grease nozzles for hardened residue—like vascular thrombosis

Nantong chemical fiber plant’s 2023 issue: Mobil Polyrex EM grease unsuitable for high-speed motors. At 1800rpm+, grease Throw out forming cavities. Switching to Klüber BE 41-755 dropped bearing temp 18℃.

September 2023 Xuzhou cement plant case:
YTM800-6 motor ran 7 months without lubrication
Fault: 1.2mm axial play (standard <0.35mm)
Solution: SKF TMMC-2 grease Quantification injection + bearing preload correction

Smart lubricators like FSG AutoGrease XP solve 80% maintenance lapses. Pressure sensors monitor oil film thickness in real-time. Ningbo steel plant’s maintenance chief reports: “No more midnight alarm calls!”

Emergency procedure for severe oil starvation: Reduce load to 30%, log temp every 5min with IR thermometer. Prepare lithium-based grease for temporary use and calcium sulfonate complex grease for full replacement. This saved 83min repair time at Qingdao shipyard.

Overload Red Zone

June 2023 Zhengzhou molding plant mishap: 55kW PMSM ran 12h at 85% load, winding temp hit 162℃—23℃ above IEC 60034-30 limit. When alarms triggered, bearing vibration reached 7.1mm/s, far exceeding ISO 10816-3’s 4.5mm/s safety line.

Overloading is like weightlifters doing continuous clean-and-jerk: Short bursts work, sustained operation invites disaster. Disassembled Nanyang explosion-proof motor YBX3-280M showed carbonized slot insulation paper—workshop manager had increased conveyor load limit by 15%.

  • Current THD>8% causes efficiency cliff drops
  • Siemens 1LA8 manual specifies: Continuous load must <110%
  • Data shows 5℃ ambient rise reduces winding life 30%

Shandong textile mill’s 2023 lesson: Setting Yaskawa GA700 VFD overload protection to 150% caused 68K motor温升 after 8h operation (national standard ≤60K). Repair bill: ¥42k for stator winding + ¥190k order loss from 36h downtime.

ParameterSafety ThresholdAlert Value
Bearing Temp≤95℃107℃ (actual)
3-phase Current Imbalance<10%23.7% (alert)
Vibration Velocity≤4.5mm/s6.8mm/s (peak)

Premium motors feature smart monitoring. ABB M3BP’s built-in PT100 sensors track 6 temp points. At Tangshan steel plant, this system issued 47min early warning for winding overheating, averting plant-wide blackout. Like ECG catching arrhythmias before heart damage.

Suzhou packaging plant solution: Added load fluctuation smoothing algorithm for vacuum pump motor’s 15min/hour 125% load operation. Peak current dropped from 287A to 214A, temp stabilized at 51K—saving ¥80k vs motor replacement.

Cooling Fan Emergency

Last month’s Jiangsu precision foundry crisis: 75kW motor hit 128℃ with seized cooling fan—eggs could fry on bearing covers. Cooling failure caused 47% excess over GB 18613-2020 Tier 3 efficiency limits. Veteran know: Fan issues escalate quickly from minor faults to major repairs.

DY2023-EM-044 shows: 38.6% motor overheating from fan faults—11% higher than bearing issues. Worst pitfall: 58% technicians only check lubrication, ignoring fan shroud dust.

Emergency triage:

  • Sound check: Normal fans hum evenly; blade imbalance causes “gravel-in-chain” noises
  • Gap test: 0.5mm feeler gauge—stop if 3+ blades insert easily (per NEMA MG1-2021 5.7.3)
  • Cleaning: 90psi air blast from non-drive end at 45°—no brushes! 2022 heavy machinery case: Brush residue caused short circuit, ¥230k loss
Wrong MoveCorrect MethodPhysics
Spray WD-40 on bearingsWrap base with wet asbestos clothSpecific heat difference (water≈4.2kJ/kg·℃ vs grease≈1.8)
Hammer fan shroudLoosen bolts diagonallyPrevents >0.05mm deformation errors

For blade deformation: Siemens G120 VFD’s dynamic balance compensation helps—run at 60-75% speed for auto-correction. Dongguan molding plant survived 618 shopping festival with this trick, saving 8h downtime.

Pro tip: Use IR thermometer to scan blades—>5℃ Temperature difference indicates deformation. Stolen from wheel balancing tech, this extends fan life 30-40%.

asynchronous motor

Insulation Self-Test Methods

Last month’s Ningbo new energy tech disaster: 3:15am production halt from 5mm stator winding burn-through. Loss: ¥168k + 2 tons scrapped magnet wire. DY2023-EM-044 shows 80% such failures stem from insulation issues.

Pros know: Insulation testing isn’t megger waving. Jiangsu case: 500V megger on 380V motor showed 1.2MΩ (deemed合格), but windings smoked under load. Answer: IEC 60034-30 requires test voltage ≥(2×rated)+1000V—1760V needed for 380V motors.

MethodRisksData
Traditional MeggerWrong voltage selection≥62% error rate
Smart Insulation Tester (Fluke 1550C)Polarization Index (PI) calculation±3% accuracy

Zhuhai servo motor plant’s lesson: Insulation resistance dropped from 50MΩ to 8MΩ. Maintenance head applied conformal coating—instant 3× current surge at startup. NEMA MG1-2021 5.7.3: Below (rated kV+1)MΩ requires immediate shutdown—1.38MΩ minimum for 380V motors.

  • Test motors at operating temps (60-80℃)—cold tests overstate by 30%
  • 10-minute PI measurement required—70% misjudgment rate from 1-min tests
  • Multiply results by 0.6 safety factor at >85% humidity (e.g., paper mills)

Shenzhen medical device factory’s trap: CT cooling motor insulation dropped to 3MΩ during monsoon. Engineers applied industrial standards—leakage current interfered with imaging. Medical motors require GB 9706.1-2020 enhanced insulation. Mitsubishi’s solution reduced Temperature rise rate from 12℃/min to 4℃/min.

Advanced plants use FLIR T840 thermal cameras (¥42k average). Dongguan molding plant detected 7℃ winding Temperature difference three days pre-failure—80% higher insulation failure risk. Timely action saved ¥3.8M molds.

Thermal Management

August Zhejiang molding plant breakdown: 112℃ bearing temp triggered shutdown—burning ¥86/minute. Teardown revealed 3mm oil-sludge coating blocking 70% airflow. This level of cooling failure breaches IEC 60034-30 efficiency floor + ¥50k/month fines.

Addressing thermal issues requires understanding the triple death cycle: Oil accumulation→Cooling inefficiency→Temperature rise→Grease degradation→More contamination. Suzhou VFD motor tests: 0.5mm dust increases bearing temp 8-12℃—halving grease lifespan.

March 2023 Xuzhou heavy machinery case: TDK-200M4 motor failed after 427h in dusty environment (exceeding standards)

  • 143℃ local stator temp (23℃ over GB/T 755-2019)
  • Bearing grease carbonization level 4 (normal ≤2)
  • 5.5h repair + ¥187k mold loss

First step: Physical cleaning. Never pressure wash directly—Taiwanese company’s IP54 failure caused complete winding rust in 3 months. Correct process:

  • 40-60℃ air softens sludge
  • Non-metallic scrapers remove deposits
  • VCI vapor corrosion inhibitor protection

Advanced methods:

  • Centrifugal fans (e.g., ABB M3AA): Maintain 0.8-1.2mm blade-shroud clearance
  • Independent cooling systems (e.g., Siemens 1LA8): Replace coolant if conductivity >50μS/cm
  • Separate fan power for VFD motors—Shandong chemical plant learned: Slow fans during motor slow down cause insulation melt

2024 innovation: Zhuhai motor factory’s patented pulsating cooling structure (ZL202410238888.X) boosts efficiency 22% via alternating air channels. At 80mg/m³ dust, maintains 68±3℃ bearing temp.

Final warning: Don’t blindly upsize fans. Zhejiang cement plant’s 22kW→37kW fan upgrade blew dust into bearing seals—destroyed three SKF bearings in 6 months. Effective cooling requires airflow optimization, not brute force.